I would have gotten nothing done today if it weren't for the fact that a solder joint on my 24-volt conversion of the dome motor had worked itself loose. I re-soldered it and all is well now.
Tomorrow I should be able to finished cutting a little more material from the foot shells and battery boxes to allow access to the ankle bolt hole on each foot. Then the feet and battery boxes can go onto the droid.
Tuesday, April 17, 2007
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